emailed david
Tested mecanum drive with tons of batteries on the tower to see if the gyro still corrected with a center of gravity that is really screwed up, worked with a fresh battery but needs a good amount of power for it to work though. Also moved some stuff around for the electrical plate that will eventually be on the back of the robot. Isaac and Thomas worked with Cole to order parts, some more parts that weren't originally on the first BOM were ordered tonight, they will be listed in the other notes section
there is an issue with teleop, when first real-time deploying a box labled "teleop elapsed seconds" starts flashing in the teleop code. Thomas searched the internet for the problem but like the "weedle" Thomas couldn't find anything.Thomas then moved all the important stuff into periodic tasks so that we could carry on testing the mecanum drive.
finish the electrical layout mentioned in work completed.
Also basically everything that was listed in Mr. Pletchers email earlier today.
sure
These things we ordered today because we didnt' realize we needed them
also we realized we have a lot more talons than previously thought so we took some off of the BOM
basically everything is in periodic tasks now so coding will probably be done from there.