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Control Systems 2014

Attendance

Note Info

Students
Mentors
Date & Time
Location & Author
  • 3/7/2014

  • 3 hours

  • Parkland Shop

  • Nolan P.


Work Completed

Discovered several bugs in the robot, wire was coming loose, PWM cable was plugged in backwards and the digital breakout card had a short and was getting hot. Gyro could have problems too. Got robot driving (again) Found the drive code wasn't running fast enough and it starved the motors.

Challenges

Communication errors with the robot and code running too slow. These have been fixed for the moment.

Work for Next Meeting

Possible driver tryouts and maybe start the autonomous coding.

On Schedule?

good