Electrical 2018
Students
Mentors
Date & Time
Location & Author
Edward K.
Aquiferland
Armeen M.
Work Completed
- Assisted drive candidate practice stuff.
- Removed broken Victor SP from Poly and replaced it with a working one.
- Shot balls at unproductive mechanical people.
Challenges
- Driving the robot up onto the platform.
- Isolating the issue involved with the faulty Victor SP.
Work for Next Meeting
- Finish calibrating drive encoders to auto can move accurate distances. See Adam's theories on Slack.
- Add rotate 90 + another drive distance to auto test.
- Switch Poly drive-distance to PID (info coming from Adam).
- Finish setting up half-field in basement, building elements if Kyle's dad drops off parts, etc.
- Attempt to align robot with vision target with Limelight (PID).
- Order hardware for the third battery.
- Continue stripping Poly2 of all useful parts.
- Decide on names for one more 2018 battery.